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Thread: boosted awd

  1. #1
    Sac DSM Member
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    Jan 2005
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    390

    Default boosted awd

    Remember, i said the lag started after the injen intake was put in? Well when we put that in we had to remove the k&n because it was too long and we replaced it with that generic filter, and since my car intake was really low (19 i think it was) I was thinking that could be the problem.

  2. #2
    Proven DSM Member
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    Jan 2005
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    Default

    Probably not, most of us run generic filters and are fine. No one wants to kick down for the K&N these days.

  3. #3
    Sac DSM Member
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    Feb 2005
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    Default

    nah i don't think that the filter would have anything to do with it. yea i have no idea why you are only pushing 19lb/min with a b16g. something isn't right. i know you are running waaaaaaaay rich (should be around .92 o2 v, you were at 1.00 o2 v!!) so you should get ahold of a logger and do some tuning. I'm guessing that since you said you have 720cc injectors and a 255 pump on a b16g, the guy that had it before you had a larger turbo on it then switched it out when he sold it to you. that would explain why you are running so rich, since you say you've never adjusted the afc.

    Its possible that your WG could be going out, or the turbo itself could be going out. I'm still puzzled as to why you were only pushing 19lbs/min..... :?

    I talked to my buddy zane, and he said he'd have to take a look at it, but from what i told him, he had no idea either. I'll get ahold of you this coming weekend and see if we can get zane to check it out, cuz i'm stumped.... :?
    Sac-DSM's one and only Flaming Troll....


    2005 Dodge NEON SRT-4 - Stage 1, AGP Wastegate, Perrin Big FMIC, MSD Wires, Perrin STS, K&N SRI, Hotchkis Springs/Sway Bars

  4. #4
    Sac DSM Member
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    Jan 2005
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    Default

    ok, i'll pull/check the vacuum lines tommorrow after work and check those hopefully one of them is damaged lol.

  5. #5
    Sac DSM Member
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    Feb 2005
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    Default

    ok, i talked to a few knowledgable dsm'ers and got a few opinions.

    First try switching the lines on your MBC. maybe when you installed the intake, you crossed the lines on accident. the MBC won't work correctly if it is backwards.

    also, check to see if your WG is stuck. attach a air compressor to the nipple on the wg. the wg actuator arm should start to move around 12psi. if it doesn't, then you have a faulty wg actuator.

    do another boost leak check while you are at it.... :D
    Sac-DSM's one and only Flaming Troll....


    2005 Dodge NEON SRT-4 - Stage 1, AGP Wastegate, Perrin Big FMIC, MSD Wires, Perrin STS, K&N SRI, Hotchkis Springs/Sway Bars

  6. #6
    Proven DSM Member
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    Jan 2005
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    888

    Default

    Low airflow numbers can be due to a faulty MAS. Small possibility.

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